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24-04-2006, 12:00 AM | #1 | ||
Banned
Join Date: Jan 2006
Location: Melbourne
Posts: 1,318
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Hey,
My car seems to be running really rough on gas (LPG) since i installed the new K & N air-filter and Tickford air-intake today, it seems to be idling very very roughly on gas when ever im stopped at lights or anywhere! I haven't tried it on petrol yet! But i will tomrrow! Does anyone know if the new air-intake and air-filter would affect the idling? Does the car have to be tuned on gas again because of the new air-intake and filter????? Cheers Simon : (Thanks to those who donated the air-filter and in-take to me! You know who you are :voldar02: ) |
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24-04-2006, 12:34 AM | #2 | ||
Regular Member
Join Date: Feb 2006
Posts: 47
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hello
have you tried resetting your ECU? other than that, maybe your leads and/or sparks are on there way out, but it could be many things. But seeing as though you upgraded your air intake, it could be your throttlebody that needs a clean out. Cheers |
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24-04-2006, 08:48 AM | #3 | ||
Just slidin'
Join Date: Sep 2005
Location: Brisvegas
Posts: 7,791
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Id say the ECU will take a couple of hundred K's to re-learn. Same thing happened with mine. I dont see why though when they are only minimal adjustments.
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MD Mondeo - For the family
NP Pajero - For the adventure |
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24-04-2006, 09:46 AM | #4 | ||
Tickford Equiped
Join Date: Jan 2005
Location: Tweed Coast
Posts: 418
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I dont know much about Gas, but wouldnt you need to get the Gas Retuned. The gas (If aftermarket dual fuel) runs its own computer that needs to be retuned. This happened to my dad landcruiser when he replaced the stock standard paper filter (Dirty) with a new stock standard paper filter. Just the increase in airflow sent the gas crazy until he got a re-tune. If its straigh gas or dual fuel from factory then i assume it runs through ecu so maybe resetting will help. But i do know an increase in air flow can send them crazy.
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Genuine Tickford Equiped 1998 AU Fairmont Mods: ....... Dash mat & Air Freshener, does that count as a mod?????? Sports Exahust, Tickford Intake Snorkle, K&N Filter, NGK Plugs, Top Gun Leads TS50 Front Bar with Fog lights, TS50 Rear Bar. Injected LPG System, |
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24-04-2006, 10:18 AM | #5 | ||
Walking with God
Join Date: Mar 2005
Location: Melbourne
Posts: 7,321
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Simon,
Give me a call, I think I may be able to help you here! GK
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2009 Mondeo Zetec TDCi - Moondust Silver 2015 Kia Sorento Platinum - Snow White Pearl 2001 Ducati Monster 900Sie - Red Now gone! 1999 AU1 Futura Wagon - Sparkling Burgundy On LPG Want a Full Life? John 10:10 |
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24-04-2006, 11:26 AM | #6 | |||
Miami Pilot
Join Date: Jan 2005
Location: ACT
Posts: 21,703
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Quote:
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24-04-2006, 02:43 PM | #7 | ||
Regular Member
Join Date: Mar 2005
Location: Gold Coast
Posts: 41
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I have a similar but opposite problem.I recently installed a new exhaust system that seems to have given me a couple of kws but now it idles really high(900- 1000).I just assumed it would need a re-tune. Any ideas?
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24-04-2006, 02:50 PM | #8 | |||
Walking with God
Join Date: Mar 2005
Location: Melbourne
Posts: 7,321
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Quote:
That's what I'd do. All the best with it. GK
__________________
2009 Mondeo Zetec TDCi - Moondust Silver 2015 Kia Sorento Platinum - Snow White Pearl 2001 Ducati Monster 900Sie - Red Now gone! 1999 AU1 Futura Wagon - Sparkling Burgundy On LPG Want a Full Life? John 10:10 |
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24-04-2006, 02:54 PM | #9 | ||
they call me Tibbo
Join Date: Dec 2004
Location: Brisbane
Posts: 6,163
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It really depends on the convertor you are using.. Some have two adjustments, a mixture screw and a sensitivity screw.. The increased volume of air might now mean the convertor needs some tweaking to match up .. Some convertors have NO manual adjustment.. Do you have a balance line fitted, did you bump it or change its position?
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24-04-2006, 03:37 PM | #10 | ||
Banned
Join Date: Jan 2006
Location: Melbourne
Posts: 1,318
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I tested it today and the car seems to only idle roughly on gas (LPG) but not petrol! Hmm i think a tune is what it needs! It's an after market set-up not a factory fit!
Cheers Simon |
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24-04-2006, 09:09 PM | #11 | ||
FF.Com.Au Hardcore
Join Date: Feb 2005
Location: Melb north
Posts: 12,025
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my mate cut holes in his airbox on his el (it ran poorly afterwards on lpg) he had to get it tuned again
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25-04-2006, 08:44 AM | #12 | ||
Spin 'em Habib !
Join Date: Jul 2005
Location: Cranbourne Victoria
Posts: 3,854
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because you were using a Paper Filter , not as much air was flowing through and hitting the gas , now with the K&N with its hyper Pourous design , 66% more air is going throuhg the airbox and hitting the gas , the reason it doesnt happen with petrol as its a Liquid and more heavy .
but thats gas for you , BBQs and Mazdas Only !! Cheers lol Daniel
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AU2PWR |
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25-04-2006, 12:32 PM | #13 | |||
Banned
Join Date: Jan 2006
Location: Melbourne
Posts: 1,318
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Quote:
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25-04-2006, 07:10 PM | #14 | ||
Spin 'em Habib !
Join Date: Jul 2005
Location: Cranbourne Victoria
Posts: 3,854
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i know , cos im smat , i mean smart
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AU2PWR |
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25-04-2006, 07:40 PM | #15 | ||
V8 Powaah
Join Date: Jan 2005
Location: Sunshine Coast, QLD
Posts: 1,994
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This one's got me interested, tell us how you go with it OzFordAU, im thinking of getting a tickford intake and K&N for my AU.
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FG G6E Turbo- Seduce & Cashmere - Sold XF S pack Sedan- AU 302 Windsor, T5, 2.77 LSD, Many Mods
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25-04-2006, 07:49 PM | #16 | ||
Spin 'em Habib !
Join Date: Jul 2005
Location: Cranbourne Victoria
Posts: 3,854
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makes a bit of a difference , but its not going to be like , WHOA BOOST , especially with LPG , Little bit more Throttle Response with the Extra Intake and Airflow !
Still Runs Alright though !! , GO GO GO
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AU2PWR |
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27-04-2006, 10:15 PM | #17 | ||
Banned
Join Date: Jan 2006
Location: Melbourne
Posts: 1,318
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Solved it! The petrol was on empty and thats why the car was running roughly! A couple of people told me not to let the petrol reading drop more then quater empty!
So i filled the petrol and gas up and its perrrfect! LOL get it Perrr....Ok bad jk lol! But it's good now! Cheer Simon :nutsycuck |
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